Several years ago we took a 96 manual FTO GPX to a place that was said to specialise in Mitsu's. Will try and cut this long long story as short as possible.
We took it there because after hard acceleration, the engine check light came on and it barely idled (rough as guts before stalling). This repair bunch claimed the whole engine has gone to Sh*t and it ended up costing us over 11 grand all up.
They claimed that they couldnt get all 6 cyls fireing so had to put in an extra ecu to handle most of the old Ecu's duties. yeah I know, sounds like A grade BS doesn't it but we didnt see that we had much choice at the time.
Anyways, it has been running OK for the past couple of years until today when it lost power and stalled... The starter motor turned the engine over just fine but it would not start... After having a good look around the engine we noticed that the "repairers" had jumpered a plug in the wiring harness and that the jumper had half fallen out... upon lifting it up to take a look, it fell out completely and we have
no idea where it goes back. Downloaded the FTO circuit diagram manuals and found the connector which originally connected to the Igntion Falure sensor but seems to have been bypassed, I assume it is no longer needed with the new ECU but must have to be Bypassed to keep the original ECU from chucking a fit???
The question is. Which two pins on the 4 pin Ignition Failure Sensor would they have bridged?? Any suggestions would be most helpful.
Attached is the circuit diagram of the IFS and its pinout.
Have been trying to understand how the IFS works, and how it connects to be able to monitor the Coils. In the second pic I have put an arrow pointing to a wire, AM I right in thinking this must be supplying a Positive Voltage to the coils whenever the ignition is ON ??
I'd really be grateful if anyone can give suggestions etc.. we would try contacting the place that did the modifications if it wasn't a weekend and we weren't 200ks away from there shop AND that I would be willing to bet that they wouldnt remember the horrible bodge job that they did anyway
