kiz wrote:vipfto wrote:could be worse and want a snow plough haha
Vipfto's turbo project
Moderators: IMC, Club Staff
- Daniel2019
- Oldtimer
- Posts: 7957
- jedwabna poszewka promocja
- Joined: Thu Jan 12, 2012 12:25 pm
- Location: Sydney!
- Contact:
Re: Vipfto's turbo project
- Attachments
-
- paddlin.jpg (4.33 KiB) Viewed 3187 times
I fix cars.
Bennoz wrote:I got Bali beli & sharted on my phone. But it was fun
bjk wrote:you old people are no help at all.
- vipfto
- Forum Moderator
- Posts: 4154
- Joined: Mon Oct 29, 2007 5:00 pm
- Location: Adelaide
Re: Vipfto's turbo project
well after spending all morning with tuner discovered that now dam wastgate is sticking and boost would only creep to 7psi at around 7000 RPM
So took her home removed turbo and dump pipe to find that the flapper was catching om dump pipe slightly so have ground out a little and put back together only to find that still not much better (its not sticking now) so little bit stumped as to why not boosting hard till way to late
Going to swap out with another new actuator next week hoping this will solve issue and also have no boost leaks at all
Worse thing is cant get her back on dyno till early next year as they shut down for xmas early
but at least tuner gave it safe tune so if I can up boost she wont blow on me
As for figures we made 144kw and just over 250nm @3500rpm early this morning before started having issues still on low boost
Had another issue pop up too now gear selector is very stiff and hard to slot into gear not sure why yet? disconnected from selector on gearobx but still same issue but will address that later as with some force can still get gears ok

So took her home removed turbo and dump pipe to find that the flapper was catching om dump pipe slightly so have ground out a little and put back together only to find that still not much better (its not sticking now) so little bit stumped as to why not boosting hard till way to late

Going to swap out with another new actuator next week hoping this will solve issue and also have no boost leaks at all

Worse thing is cant get her back on dyno till early next year as they shut down for xmas early


As for figures we made 144kw and just over 250nm @3500rpm early this morning before started having issues still on low boost

Had another issue pop up too now gear selector is very stiff and hard to slot into gear not sure why yet? disconnected from selector on gearobx but still same issue but will address that later as with some force can still get gears ok
FTO GR-TURBO
172KW ATW @ 11PSI
172KW ATW @ 11PSI
- ZFL45H1
- Oldtimer
- Posts: 1830
- Joined: Sun Feb 07, 2010 6:00 pm
- Location: Albury
Re: Vipfto's turbo project
For a low boost setting that's nice Im looking forward to mine more and morevipfto wrote:
As for figures we made 144kw and just over 250nm @3500rpm

gotta get there one day :)
- Bennoz
- National President
- Posts: 23676
- Joined: Fri Jan 21, 2005 6:00 pm
- Location: Sydney
- Contact:
Re: Vipfto's turbo project
Cooked the grease in the tubevipfto wrote:Had another issue pop up too now gear selector is very stiff and hard to slot into gear not sure why yet? disconnected from selector on gearobx but still same issue but will address that later as with some force can still get gears ok

- vipfto
- Forum Moderator
- Posts: 4154
- Joined: Mon Oct 29, 2007 5:00 pm
- Location: Adelaide
- Astron_Boy
- Trolling Gen Y
- Posts: 8400
- Joined: Sun May 27, 2007 5:00 pm
- Location: Wine Country NSW
- Contact:
Re: Vipfto's turbo project
Now the build has begun!vipfto wrote:well after spending all morning with tuner discovered that now dam wastgate is sticking and boost would only creep to 7psi at around 7000 RPM![]()
So took her home removed turbo and dump pipe to find that the flapper was catching om dump pipe slightly so have ground out a little and put back together only to find that still not much better (its not sticking now) so little bit stumped as to why not boosting hard till way to late![]()
Going to swap out with another new actuator next week hoping this will solve issue and also have no boost leaks at all![]()
Worse thing is cant get her back on dyno till early next year as they shut down for xmas earlybut at least tuner gave it safe tune so if I can up boost she wont blow on me
![]()
As for figures we made 144kw and just over 250nm @3500rpm early this morning before started having issues still on low boost![]()
Had another issue pop up too now gear selector is very stiff and hard to slot into gear not sure why yet? disconnected from selector on gearobx but still same issue but will address that later as with some force can still get gears ok
Took a while, but we got there.


- vipfto
- Forum Moderator
- Posts: 4154
- Joined: Mon Oct 29, 2007 5:00 pm
- Location: Adelaide
-
- 9.5"
- Posts: 6793
- Joined: Tue Oct 13, 2009 5:00 pm
Re: Vipfto's turbo project
Could get a cable luber?
Also your not missing any of the rubber grommets where it the bracket attaches to the gearbox?
Also your not missing any of the rubber grommets where it the bracket attaches to the gearbox?
- vipfto
- Forum Moderator
- Posts: 4154
- Joined: Mon Oct 29, 2007 5:00 pm
- Location: Adelaide
- vipfto
- Forum Moderator
- Posts: 4154
- Joined: Mon Oct 29, 2007 5:00 pm
- Location: Adelaide
Re: Vipfto's turbo project
interesting worth noting too is once wastgate failed did a run whilst basically N/A and still run up 121kw not too bad me thinks. Tuner still says 160 should be very acheivable
FTO GR-TURBO
172KW ATW @ 11PSI
172KW ATW @ 11PSI
- Kustom
- Oldtimer
- Posts: 6144
- Joined: Sun Oct 04, 2009 5:00 pm
- Location: Brisbane
- vipfto
- Forum Moderator
- Posts: 4154
- Joined: Mon Oct 29, 2007 5:00 pm
- Location: Adelaide
Re: Vipfto's turbo project
well after much f**king round all boosting sweet again and dam hard too. hoping to get back to tuner next week if he can squeeze me in otherwise will have to wait till new year before final tune. Now hitting 5 psi @ 2500 rpm and climbing . Worst thing is now gear changes rather hard till can swap out cables
FTO GR-TURBO
172KW ATW @ 11PSI
172KW ATW @ 11PSI
- aza013
- NSW Coordinator
- Posts: 9089
- Joined: Mon Mar 26, 2007 5:00 pm
- Location: The Shire
- Contact:
Re: Vipfto's turbo project
Sounds like you have a weapon now
.
Great work.

Great work.
- Bennoz
- National President
- Posts: 23676
- Joined: Fri Jan 21, 2005 6:00 pm
- Location: Sydney
- Contact:
Re: Vipfto's turbo project
Is this you Tim? 



- vipfto
- Forum Moderator
- Posts: 4154
- Joined: Mon Oct 29, 2007 5:00 pm
- Location: Adelaide
- vipfto
- Forum Moderator
- Posts: 4154
- Joined: Mon Oct 29, 2007 5:00 pm
- Location: Adelaide
Re: Vipfto's turbo project
All booked in next week hoping new actuator arrives before she goes in basically not sure how high it will boost atm so not driving again till been on dyno again. Did take vid of last time but wasn't power run. Will try get down there again next week for last runs
FTO GR-TURBO
172KW ATW @ 11PSI
172KW ATW @ 11PSI
- vipfto
- Forum Moderator
- Posts: 4154
- Joined: Mon Oct 29, 2007 5:00 pm
- Location: Adelaide
Re: Vipfto's turbo project
Been a while since update but got final tune done before xmas and hit 160 @ wheels have scaled back to 158 for safe tune currently running @9psi its f**king awesome. Get a little torque steer but to be expected, Had issues getting the timing right as was knocking round 4.5-5k mark but all sorted was just some bad connections.
Tuner has also now reccomended to go to standalone motec or haltec unit but I dont reall y wanna spend that kind of money now although he said there is much more potential there just being held back by ECU. Only prob is that also means having to decomp and forge internals which also means more $
So will park her up for now till heat goes and then be driving again after summer seeing as have no A/C etc
But sh*t does it give a great feeling esp being able to fry up the rubber just by boosting hard in 2nd with cold tyres
Tuner has also now reccomended to go to standalone motec or haltec unit but I dont reall y wanna spend that kind of money now although he said there is much more potential there just being held back by ECU. Only prob is that also means having to decomp and forge internals which also means more $
So will park her up for now till heat goes and then be driving again after summer seeing as have no A/C etc
But sh*t does it give a great feeling esp being able to fry up the rubber just by boosting hard in 2nd with cold tyres

FTO GR-TURBO
172KW ATW @ 11PSI
172KW ATW @ 11PSI
- aza013
- NSW Coordinator
- Posts: 9089
- Joined: Mon Mar 26, 2007 5:00 pm
- Location: The Shire
- Contact:
- Bennoz
- National President
- Posts: 23676
- Joined: Fri Jan 21, 2005 6:00 pm
- Location: Sydney
- Contact:
Re: Vipfto's turbo project
Result! 

-
- Oldtimer
- Posts: 1394
- Joined: Wed Jan 19, 2011 11:32 pm
- Location: Perth
- Contact:
Re: Vipfto's turbo project
Well done mate.
Sorry to go over old ground but you're at 9psi with standard compression and standard internals right?
I bet you have a huge grin every time you drive her.
Sorry to go over old ground but you're at 9psi with standard compression and standard internals right?
I bet you have a huge grin every time you drive her.